Observed increase clearance on the left cylinder exhaust valve. Set to spec and now valve chatter has reduced greatly - however this valve is quite a bit louder than the others when cold even with the correct adjustments made. So, likely have some light rocker damage but when the bike is warmed it sounds quite nice, a little excess chatter under load for that valve but it still runs strong.I should add that you should try adjusting the valves again to see if any have excess clearance. That will tell you if any excess wear happened, and hopefully you can adjust most of the noise out of it but it remains to be seen.
Glad it's running well, and the excess wear on the rocker arms will make valve adjustments more difficult to set correctly but as long as the noise is not offensive then you're about as well off as one could expect under the risky circumstances that occurred.Observed increase clearance on the left cylinder exhaust valve. Set to spec and now valve chatter has reduced greatly - however this valve is quite a bit louder than the others when cold even with the correct adjustments made. So, likely have some light rocker damage but when the bike is warmed it sounds quite nice, a little excess chatter under load for that valve but it still runs strong.
Adjusted the cam chain as well?This included a full retune up - valves, timing and points gap, two oil changes and we cleaned the oil filter as well.
You're very welcome, it's what we do here and it's what makes VHT different than so many other forums. Glad the results of the incident were repairable.I am very grateful to you, ancientdad, for guiding me and this community - you’ve been a huge help, thanks.

Hard to tell from the picture where the cable connects to the battery. Is the bolt on the top of the terminal or on the front facing the tank? Could you drill a new hole in what left and connect to the battery with maybe a spacer between the battery terminal and the cable lug.

That bolt is not hard to take out. And it should just be on the “nut” end of the upper engine mount.View attachment 55902
Here’s what I did, it is working much better now. Squished the contact with washers to increase contact area. Temporary fix, I think I’ll either modify the current or replace it.
In the event that I replace it, the other side of the ground is grounded through a bolt that goes through the engine. I suspect that bolt is hard to take out, anyone have advice on how I’d go about replacing the whole wire?
Thanks for your advice!
I’ve ordered the deluxe rebuild kit from 4into1, my intention is to replace only aftermarket brass and keep what is original. Will update with results!The bike has been running great lately, but there’s been an underlying issue since I got it; the engine bogs at 7k rpm and then picks up again and accelerates strongly to redline. I am convinced it’s a fuel issue. I’ve cleaned them thoroughly, but the last time I was cleaning I discovered the right side carb has a #68 jet while the left side was sporting a #70. I figured this was my issue, so I’ve replaced it with a NOS Keihn #68 jet but bog at 7k is still there, though the bike feels more confident in general accelerating since replacing the jet.
Any ideas what my issue could be? I figure it must be an issue with the main jets as it’s so late in the power band - but now that I think of it I am starting to suspect a previous owner botched a rebuild and the jets are all sorts of messed up. It would explain why my bike needs to have the pilot screw all the way in to idle at 1100 rpm if the pilot jet is the incorrect size. I think the next step is replacing all the jets with a rebuild kit - could someone point me in the best direction for a high quality one?
Any other ideas about this issue? it’s been present through timing changes, valve adjustment, everything. Running stock airboxes and exhaust.
Filters are new and OEM! Appear to still be quite clean after 1500 miles. I’m thinking fuel because the bike picks up again after the bog at 7k and pulls very smoothly up to 9.5k, sounds to me like a troubled jet. I will test it without filters briefly to see if anything changes, but I’d expect it to run quite lean. Thanks for your input!What kind of shape are the filters in? May be airflow, not just the fuel side of fuel/air mixture.
May want to give it a whirl without the filters for a quick trial run.
Carburetors semi-rebuilt per visual inspection of wear and tear and originality to the 722A carbs.Filters are new and OEM! Appear to still be quite clean after 1500 miles. I’m thinking fuel because the bike picks up again after the bog at 7k and pulls very smoothly up to 9.5k, sounds to me like a troubled jet. I will test it without filters briefly to see if anything changes, but I’d expect it to run quite lean. Thanks for your input!

True. However the hole placement and sizing is a critical factor.From my understanding the secondary emulsifiers aren't in play at idle so shouldn't have any effect on pilot circuit.
Thinking I’ll just replace everything that doesn’t have the Keihin stamps and see how it feels. So far the replacement parts have done nothing but help. I’m going to also make sure all the air bleeds are clear but I swear I have been thorough with my cleaning haha!True. However the hole placement and sizing is a critical factor.
Trust but verify.but I swear I have been thorough with my cleaning haha!
Upon further riding, I am frustrated. The bike now has issues above 6k rpm, it feels rough, sluggish, and like it’s running out gas (I have a full tank). I’m lost though because I just rebuilt the carbs again this morning but the only change I made was to the needle seat, needle jet, #35 idle jet, and I cleaned everything thoroughly. The bike idles decently but at stops the rpm’s drop to 800 and it almost dies without a little bit of throttle.Here is a video of the pilot screw behavior (acting like an on and off switch for a high idle when bottomed out). Besides this, it’s running quite well on factory specs and has a smooth idle. I believe the culprit of my issues was a worn needle jet on the right carb, the tip was worn and angled.
oh and the tube and rim strips were replaced.

Alright well this last rebuild was my last it seems. I got off work and decided to rebuild the carburetors after seeing the ebay listing (thanks) showing main jet emulsion tubes with the little hole a tiny bit lower than the ones I put into my carburetor and figured that cannot be right.Lowering the float height to 25mm would make the idle richer, since that would raise the fuel level in the bowl.
The left carb mixture screw seemed to be acting strangely in the video of post #71 — sounded rich to me. I assume this was not happening on the right? The left carb has replacement brass. I would focus on acquiring original brass for the left side and trying to put everything in the carbs to factory settings. Then, go from there.
Sometimes you can find parts lots on eBay, like this one. I did not check the contents of this listing carefully. I have also purchased used carbs and rebuilt those or swapped parts between different carbs.
Glad you finally got it sorted. Now don't let it sit and gum up the carbs again, and you'll be golden!Alright well this last rebuild was my last it seems. I got off work and decided to rebuild the carburetors after seeing the ebay listing (thanks) showing main jet emulsion tubes with the little hole a tiny bit lower than the ones I put into my carburetor and figured that cannot be right.
First, I checked spark plugs. Left was dark and sooty, right was white and chalky. Yeah, it was feeling awful so no surprises there.
So, I replaced both main jet emulsion tubes with the ones that came on the bike, set both floats to 26.5mm, and cleaned the pilot screw circuit a little more. I was very careful in installing its oring and washer. I also cleaned a small airway that vents into the world I assume for excess air pressure in the float bowl.
Something here fixed it. No more high end problems, idles at factory spec. 3/4 of a turn out from bottom on both sides and I get a nice even idle. Not perfect, but with some fine tuning I bet it will be. And all it took was 5 consecutive rebuilds!


Seems like a good plan.Rich at idle, lean at high rpm feels like I should up the main jets to 110s which I have on hand and then raise the float to 26mm again.


Coils were either replaced by the previous owner or are original to the bike. I’ll swap them left for right and see if the condition swaps cylinders.It's definitely worth considering the ignition components. Sometimes a coil will fail under heavy load, yet work under normal load. This can also stem from issues with the charging system not keeping up under heavy load.
Can you remind us about your ignition coils? Type? Age?
You might not have to physically swap them, just swap plug wires and yellow and blue wires from the points.Coils were either replaced by the previous owner or are original to the bike. I’ll swap them left for right and see if the condition swaps cylinders.
Are they the blue or possibly off-white Tek coils?Coils were either replaced by the previous owner or are original to the bike. I’ll swap them left for right and see if the condition swaps cylinders.
View attachment IMG_5216.jpegAre they the blue or possibly off-white Tek coils?
That is original, condensers too. And BTW, I'm a dad and I'm older than those coils.View attachment 57112
Here’s an older picture of the condenser / coils
Looks like it’s about as old as my dad.
And it's Nippon Denso rather than Tek. Old doesn't mean bad and new doesn't mean good, but it's probably worth trying the swapped leads to explore the coil function further.View attachment 57112
Here’s an older picture of the condenser / coils
Looks like it’s about as old as my dad.
Okay I’d like to try this, so the yellow and blue wires coming from the points swap into the yellow and blue wires coming from the coils.You might not have to physically swap them, just swap plug wires and yellow and blue wires from the points.
